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Kasus Perusahaan Tentang Case Study: Upgrading Industrial Emulsion Production Efficiency and Quality with Advanced Emulsification Equipment

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Case Study: Upgrading Industrial Emulsion Production Efficiency and Quality with Advanced Emulsification Equipment

2025-12-23

Case Study: Upgrading Industrial Emulsion Production Efficiency and Quality with Advanced Emulsification Equipment

In the industrial manufacturing landscape, emulsion products serve as foundational materials across sectors including architectural coatings, industrial adhesives, textile auxiliaries, and food processing. The quality of industrial emulsions—characterized by droplet size distribution, phase stability, and component uniformity—directly determines the performance of end products. This case study focuses on the application of advanced industrial emulsification equipment in resolving long-standing process challenges in the production of high-performance water-based architectural coating emulsions, detailing the equipment selection, process optimization, and tangible outcomes achieved without compromising operational compliance and scalability.

1. Background and Core Process Challenges

The production process of the target water-based architectural coating emulsion involved two immiscible phases: an oil phase consisting of acrylic monomers, coalescing agents, and hydrophobic modifiers, and an aqueous phase containing deionized water, emulsifiers, initiators, and pH regulators. Prior to the adoption of new emulsification equipment, the manufacturing process relied on traditional anchor-type stirring tanks, which led to four critical challenges that restricted production capacity and product competitiveness:
First, inadequate dispersion of oil-phase monomers. The acrylic monomers in the oil phase had high viscosity and poor wettability. During traditional stirring, the monomers tended to form large droplets or agglomerates that could not be fully broken down. These undispersed particles remained in the final emulsion, resulting in "fish eyes" (visible solid particles) in the coating film, which severely affected the film's smoothness and durability.
Second, inconsistent droplet size distribution. The low shear force generated by anchor-type stirrers failed to achieve uniform dispersion of the two phases. Quality testing data showed that the droplet size D90 (the size at which 90% of droplets are smaller) of the emulsion fluctuated between 15 μm and 30 μm, far exceeding the industry-accepted range of 5 μm to 10 μm. This inconsistency led to significant variations in the viscosity and stability of the emulsion, with some batches showing oil separation within 7 days of storage and others exhibiting excessive viscosity that hindered application.
Third, low production efficiency and high energy consumption. To compensate for the insufficient shear force, the traditional process required prolonged stirring times—each 5-ton batch took approximately 6 hours to complete emulsification. The extended operation not only reduced production throughput but also increased energy consumption, with the stirring system consuming an average of 120 kWh per batch. Additionally, the poor stability of intermediate products led to a qualification rate of only 82%, resulting in substantial waste of raw materials and labor costs.
Fourth, difficulty in scaling up production. The traditional batch stirring process relied heavily on manual operation to control feeding speed and stirring intensity. When scaling up from laboratory-scale (50L) to industrial-scale (5-ton) production, the process parameters were difficult to replicate accurately, leading to significant quality differences between pilot and mass-produced batches. This scalability issue limited the expansion of production capacity to meet growing market demand.
Furthermore, the production process needed to comply with industrial safety and environmental standards, requiring the equipment to be constructed with corrosion-resistant materials, equipped with effective sealing systems to prevent monomer volatilization, and compatible with clean-in-place (CIP) systems to ensure operational hygiene.

2. Equipment Selection and Process Optimization

After a comprehensive assessment of process requirements, product specifications, and scalability needs, a multi-stage industrial emulsification system was selected, consisting of a pre-dispersion mixer and a pipeline-type high-shear emulsifier. The equipment selection was guided by the principles of enhancing shear efficiency, ensuring process controllability, and facilitating seamless scale-up, with key technical features tailored to the characteristics of water-based acrylic emulsions:
1. Pre-dispersion Mixer: Equipped with a high-speed rotating impeller and a turbulence-generating baffle, this mixer was designed to break down large agglomerates in the oil phase before primary emulsification. Constructed from 316L stainless steel, it featured a smooth inner wall with a surface roughness Ra ≤ 0.4 μm to prevent material adhesion. The mixer’s variable frequency drive (VFD) allowed the rotational speed to be adjusted between 500 rpm and 3000 rpm, enabling precise control of dispersion intensity based on the viscosity of the oil phase.
2. Pipeline-type High-Shear Emulsifier: As the core equipment, it adopted a three-stage rotor-stator structure with a minimum gap of 0.05 mm between the rotor and stator. This design generated intense shear forces (up to 10^6 s^-1), cavitation, and impact effects to further refine the droplet size. The emulsifier’s flow rate could reach 8 m³/h, supporting continuous on-line emulsification and circulation. It was also integrated with a real-time monitoring system to track key parameters such as rotational speed, pressure, and temperature, with data logging capabilities for process traceability. The equipment’s seal design (mechanical seal with cooling system) prevented monomer volatilization, meeting environmental and safety requirements.
Based on the new equipment, the production process was optimized into four key stages to ensure consistency and efficiency:
1. Pre-dispersion Stage: The oil-phase materials (acrylic monomers, coalescing agents, hydrophobic modifiers) were added to the pre-dispersion mixer, and the impeller was activated at 2500 rpm to create a high-turbulence flow field. This process broke down initial agglomerates and formed a uniform, low-viscosity oil phase within 30 minutes, eliminating "fish eye" formation at the source.
2. Controlled Feeding Stage: The pre-dispersed oil phase and aqueous phase (deionized water, emulsifiers, initiators) were pumped into the pipeline-type emulsifier at a fixed volume ratio (1:3) via metering pumps. The feeding speed was precisely controlled by the VFD system to ensure a stable ratio, avoiding phase inversion caused by sudden changes in material composition.
3. Multi-cycle Emulsification Stage: The initially emulsified mixture was circulated through the pipeline-type emulsifier for 2-3 cycles, with each cycle lasting approximately 45 minutes. The three-stage rotor-stator structure ensured that the droplet size was gradually refined during each circulation, and the real-time monitoring system adjusted the rotational speed (2000-4000 rpm) based on pressure feedback to maintain optimal shear intensity.
4. Post-Emulsification Stabilization Stage: After completing the multi-cycle emulsification, the emulsion was transferred to a holding tank for post-processing (pH adjustment, defoaming). The holding tank was equipped with a low-speed stirrer to maintain homogeneity without damaging the refined droplets. The entire process was semi-automated, with only minimal manual intervention required for parameter confirmation.

3. Implementation Outcomes and Performance Verification

Following the deployment of the advanced emulsification system and optimized process, continuous production data (collected over 6 months) and third-party quality testing confirmed significant improvements in product quality, production efficiency, and scalability. The key outcomes are as follows:
Product Quality Enhancement: The droplet size distribution of the emulsion was significantly refined and stabilized. Test results showed that the D90 of the emulsion was consistently controlled between 6 μm and 9 μm, meeting the industry’s high-performance standards. The "fish eye" defect rate in the final coating film was reduced from 15% to less than 1%. Stability testing indicated that the emulsion showed no oil separation, sedimentation, or viscosity variation after 30 days of storage at 50°C (accelerated aging test), and the shelf life was extended from 6 months to 12 months. Additionally, the uniformity of component distribution was improved, with the relative standard deviation (RSD) of acrylic monomer content in different samples reduced from 4.1% to 0.9%.
Production Efficiency and Cost Reduction: The total processing time per 5-ton batch was reduced from 6 hours to 2 hours, representing a 66.7% increase in production efficiency. The production capacity was scaled up from 20 tons/day to 50 tons/day, effectively meeting market demand. Energy consumption per batch was reduced from 120 kWh to 55 kWh, a 54.2% reduction in energy costs. The product qualification rate increased from 82% to 99%, minimizing raw material waste and reducing production costs by approximately 28%.
Scalability and Process Compliance: The semi-automated control system ensured that process parameters (feeding ratio, rotational speed, temperature) could be accurately replicated across different production scales (from 50L pilot to 5-ton industrial batches), eliminating quality differences between scales. The 316L stainless steel construction and CIP compatibility of the equipment simplified cleaning procedures, reducing cleaning time by 40% and ensuring compliance with industrial hygiene standards. The mechanical seal and exhaust treatment system prevented monomer volatilization, meeting environmental emission requirements.
Equipment Reliability: During 6 months of continuous operation, the emulsification system maintained stable performance with no unplanned downtime. The maintenance cycle was extended from once every 1 month (traditional equipment) to once every 6 months, reducing maintenance costs by 75%. The modular design of the equipment also facilitated easy replacement of wear parts (e.g., rotor, stator), minimizing maintenance time and operational disruption.

4. Key Insights and Conclusion

This case study demonstrates that advanced industrial emulsification equipment, when paired with optimized process design, can effectively address the core challenges of traditional emulsion production—poor dispersion, inconsistent quality, low efficiency, and scalability issues. The success of this implementation lies in three key insights:
First, pre-dispersion is a critical precursor to high-quality emulsification. Targeted pre-dispersion of high-viscosity oil-phase materials eliminates agglomerates at the early stage, reducing the load on subsequent emulsification steps and improving overall process efficiency. Second, multi-stage high-shear emulsification with real-time monitoring ensures precise control of droplet size distribution, which is the key to enhancing emulsion stability and end-product performance. Third, semi-automated and scalable equipment design is essential for industrial production, enabling consistent parameter replication across scales and reducing reliance on manual operation.
In conclusion, the adoption of the multi-stage industrial emulsification system has not only resolved the specific process challenges faced in water-based architectural coating emulsion production but also established a stable, efficient, and scalable production process. This implementation provides a valuable reference for industrial manufacturers seeking to upgrade emulsion production lines, highlighting the role of advanced equipment in driving quality improvement, efficiency enhancement, and cost reduction in industrial emulsion manufacturing.